Ankita Patale, Tushar A Shinde* and Raichurkar PP
SVKM’s NMIMS, Centre for Textile Functions, India
*Corresponding author: Tushar A Shinde, SVKMS, NMIMS, Centre for Textile Functions, Mukesh Patel School of Technology, Management Shirpur, District Dhule-425405, India
Submission: August 18, 2018;Published: October 23, 2018
ISSN 2578-0271 Volume4 Issue4
Textile manufacturing is a complex process and it is affected by various parameters. Most of the defect in the fabric is either highlighted or covered in especially in dyeing department. We are follow in this experiment is to identify the important objectionable defect in the terry towel produced in the winch Thies dyeing machine. This research work is done for preventing the defect in processing & weaving department (excluding spinning department). This study aims to report a root cause analysis of the major defect. This study helps in root cause analysis of the entire process in reducing the defect. It has been reported by many others that careful consideration of process parameter helps technical person to ensure the same faults do not occurs.
This study reviles important process parameters such as pretreatment and its effect on absorbency to make uniform dyeing. This study tries to found the terry towel dyeing defect such as uneven dyeing, staining, lintting, shearing, bowing and holes and how we can minimize and neglect this faults to taking remedies. This report contains work done by various workers and technician in dyeing. Experiment conducted in “Thies” dyeing machine clearly shows how to reduce major objectionable defect in terry towel dyeing. This report contains the important content of parameters and their effect in the reducing the defect significantly. This project is able to give a deep concept about terry towel dyeing faults in soft flow dyeing machine, causes and their remedies and carried out to minimize the dyeing defect by taking particular corrective action Thus, this study enrich knowledge on dyeing, produce faults free terry towel in modern textile plant.
Keywords: Quality; Defects; Productivity; Remedies; Dyeing faults
If product fulfills the customer expectation, the customer will be pleased and consider that the product is acceptable and of high quality. If their expectation is not fulfilled, then customer will consider that the product is of low quality (down grade).
Product must be of high quality as much as enough to meet customer requirements. When quality cost is investigated, defect cost is great disadvantages for product cost . The aim of this project is to minimizing the dyeing defect. If these are minimized it is possible to decrease along with increase in production speed. Most of the time is spend in dyeing department for this reason. The dyeing department is most important one concerning production quality study. The defects which are occurred in dyeing department due to various reason, the causes of these defects are determined by defect study. When the causes of these defects are eliminated, the production with better quality (A grade) is achieved.
We are used the material for the experiment was 100% cotton terry towel, which is already prepared from weaving department (excluding for spinning department). So, we are basically focused on the causes & remedies of following department .
b) Grey Folding
c) Chemical Processing
d) Finish folding
a) We collected previous data about defect arises in dyeing section.
b) We analyzed data for causes of defect found .
c) We took corrective action to minimize the defect by taking precautions in experimental methods.
d) Then collected the data again and analyzed for defect.
e) Trials taken for 25 day and compare the defect by using following unit.
Sewing defect: These defects are usually caused by errors arising from wrong functioning of sewing machine.
Seaming defect: These defects are usually caused by errors arising from the interaction of the operator and machine in the handling of terry towel.
Fabric defect: These are caused by errors from the fabric processing like pretreatment and dyeing.
Defective pieces: Defective pieces are those pieces, which contain above defects and are separated for alteration during checking.
Quantitative measure of defect there are two measuring units as below.
a) Defect per hundred units
b) Percent defectives
A. Man related defect
B. Machine related defect
C. Material related defect
A. Man related defect: The man related defects mean due to improper handling of materials the defect occurs are like stains, yellow pen marking, colors stains, patchy dyeing, length and cross cut, selvedge cut etc.
B. Machine related defect: The machine related defects are like shearing, bowing, missing end, pile pulling, cracks, half pieces, reverse terry, lining, etc.
C. Material related defect: The material related defect is like contamination, lintting, etc.
Defect in Dyeing department .
Stain: Stains are classified in five types.
a) Soil or mud stain
b) Rust and bit stain
c) Oil stain
d) Contamination stain
e) Softener stain
f) Color stain
Causes Soil or mud stains:
i. Improper material handling by workers.
ii. Material in contact with dust present part of machine, trolley, etc.
i. Care must be taken during material handling by workers.
ii. To avoid material in contact with dusty part of machine, trolley etc.
Figure 1:Defect of rust and bit stains.
Causes rust and bit stains:
i. Unloading of dyed material in without cover trolley (uncover) and transferring it to next process.
ii. This is occurring when material is in contact with rust present roller on rope opener, shearing machine and trolleys.
iii. Bit stain occurs due to sparrows present in the plant (Figure 2A & 2B).
Remedies rust and bit stains:
Figure 2A:Causes of rust and bit stains.
Figure 2B:Causes of rust and bit stains.
i. Loading or unloading the material in full polypropylene sheet covered trolley and then transfer to next process.
ii. Proper cleaning and washing of rope opener and shearing machine and trolleys etc.
Figure 3A:remedies of rust and bit stains.
iii. Material must be properly covered with polythene before transfer to next process (Figure 3A & 3B).
Figure 3B:Causes of rust and bit stains.
Causes of oil stain:
i. Oil stains may be occurring from weaving on selvedge of terry towel due to temple and cutter.
ii. Due to use of excessive oil in dyeing section.
iii. Excessive oil use in stitching machine also causes to oil mark on terry towel (Figure 4).
Figure 4:Defect of oil stain.
Remedies of oil stain:
i. Daily checking the part of weaving machine and properly clean the machine.
ii. Material should be handle carefully from oily part of machine, trolley etc.
iii. Material should be handle carefully by workers on stitching machine and machine must be clean properly.
Figure 5:Remedies of oil stain.
iv. Check grey Material coming from weaving before pretreatment (Figure 5).
Causes of Contamination:
i. This stain occurs due to impurities present in row cotton material and it remains as it is up to yarn stage.
Remedies of Contamination:
i. Use impurity less row material of cotton.
Figure 6:Defects of softener spot.
Causes of softener spot:
i. Improper softener dissolving in the addition tank with water.
ii. Improper dosing and poor emulsification of softener applied.
iii. Foam present on material may causes softener spot.
iv. Inferior quality of softener.
v. If pH is not maintaining.
i. Proper or uniformly dissolving of softener in addition tank with water
ii. Proper dosing of softener.
iii. Foam completely removes from fabric.
iv. Use right softener and the correct procedure of application.
v. Maintain pH.
f) Color spot or stain (Figure 7)
Figure 7:Defects of color Spot.
Causes of color spot:
i. Improper machine cleaning (hydro extractor, rope opener)
ii. Improper material handling by workers.
iii. Improper mixing and dissolving of dyestuff.
iv. Dye bath hardness.
i. Proper machine cleaning.
ii. Proper material handling by worker with hand gloze.
iii. Mixing and dosing of dyestuff should be properly.
iv. Water of dye bath should hardness free (Figure 8A & 8B).
Figure 8A:Remedies of color spot.Defects of color Spot.
Figure 8B:Remedies of color spot.
Figure 9:Defect of dyeing hole.
Causes of dyeing hole:
i. Improper scouring and bleaching.
ii. Improper peroxide and caustic dosing.
iii. Due to over bleach.
iv. Improper material handling may causes hole on the fabric.
i. Enzyme should be done carefully.
ii. Caustic dosing must be slow.
iii. Avoided over bleach of material.
Figure 10:Linttin defect.
Causes of Linttin defect:
i. Improper sizing.
ii. Also due to use of low twist yarn in terry weaving
Remedies of Linttin defect:
i. Only minor floats can be rectified.
Figure 11:Defect of bowing.
Causes of bowing defects:
i. Improper speed of dryer Cylinder.
Remedies of bowing defects:
i. Set proper speed for particular GMS of terry towel.
Figure 12:Defect of shearing.
Causes of Shearing:
i. Improper distance between spiral blade of shearing machine and material.
ii. Mechanical problem.
iii. Operator problem.
Remedies of Shearing:
i. Set proper distance between spiral blade and material.
ii. Operator should be trained and must be careful.
Figure 13:Defect of uneven dyeing (Patchy).
Causes of uneven dyeing (Patchy):
i. Uneven pretreatment (desizing, scouring and bleaching).
ii. Very rapid addition of dyes and chemicals.
iii. Lack of controlling dyeing parameters.
Remedies of uneven dyeing (Patchy):
i. By ensuring pretreatment.
ii. Proper addition of dyes and chemicals.
iii. Controlling all dyeing parameters.
Process control parameters to avoided uneven dyeing: pH, Time, Temperature, Liquor ratio, Water hardness, Chemical dosing time, H2O2 killing.
Figure 16:Defect of percentage in all departments.
Figure 17:Defect of percentage in all departments.
Before trial result of defect in processing department (Figure 18):
After trial result defect in processing department (Figure 19):
In this project we try to minimize the dyeing defect arising in the processing department. For this work first we study and analyze that which defects are occurs in terry towel production and their quantity by collecting back month data of downgrade in overall terry towel production . After this we calculate % wise defectives in various department.
Then we focus on defect arising in processing department. By our above analysis processing defect was found in 0.7% of total CTN packing (Pcs) in which stain was found in large quantity 19.7%, Shearing 4.5%, Lintting 1.9% , Bowing 0.5%, uneven dyeing(patchy) 0.3% and holes found 7.2% Near by one month we are continue this work and then after discussion with our industrial mentor we try to goes towards the origin of defect and suggest the remedies for defect occurs in processing department [7,8]. After taking corrective action by implementation of our remedies we start work for minimization of defect near by one month. After completion of work we analyze again quantity of defect in processing department which is slightly minimize than before trial defect percent in which stain was found 13.5%, shearing 2.5%, bowing 0.06%, patchy dyeing 0.2% and holes 5.5%. After comparing it with previous data of defect our project work minimizes the processing defect from 0.7% to 0.3% i.e we minimize 0.4% defect in processing department [9,10].
In this project from our above analysis the defect coming from processing department was minimize as follow:
i. In conventional process of industry stains was coming 19.7% and after our project work and implementation of our suggested remedies it is minimize to 13.5%.
ii. Shearing was coming 4.5% and after implementation of remedies it is minimize to 2.5%.
iii. Bowing was coming 0.5% and after implementation remedies it is minimized to 0.06%.
iv. Uneven dyeing (patchy) was coming 0.3% and after implementation of remedies it is minimize to 0.2%.
v. In conventional industrial process of industry, a hole is coming 7.2% and after our studies and action taken it is minimized to 5.5%.
From our above report we concluded that before taking corrective action overall percentage of processing defect was 0.7%. After taking corrective action in processing department by implementation of our remedies, defect coming from over all processing department was 0.3%. Defect arising in processing department were under controlled and minimizing by 0.4% differences. In this project it was also concluded that most of the processing defect were coming due to manual operation during unloading and loading processing.
© 2018 Tushar A Shinde . This is an open access article distributed under the terms of the Creative Commons Attribution License , which permits unrestricted use, distribution, and build upon your work non-commercially.